yewly1990
Known Member
So yewly1990's problem fix already? Or the engine exploded due to insufficient fueling with full boost in closed loop.
My problem fixed, a/f ratio too lean, and ignition timing not correct by previous tuner.
So yewly1990's problem fix already? Or the engine exploded due to insufficient fueling with full boost in closed loop.
My problem fixed, a/f ratio too lean, and ignition timing not correct by previous tuner.
My problem fixed, a/f ratio too lean, and ignition timing not correct by previous tuner.
Which tuner now?
And Previous tuner charge every time you go back.......
Puchong RS dyno
---------- Post added at 06:53 PM ---------- 6 hour anti-bump limit - Previous post was at 06:53 PM ----------
Nowdays most tuner are good businessman
I tuned my swift BOT at RS too, robyn. I ask him and he said he pulled timing and add more fuel trim at higher boost/rpm/load for safety.That might explain why your knock gone when timing is pulled. I'm using bigger injector oppose to yours 1 extra injector.btw
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